The nozzle was made of 2 main pieces joined by a combination of bolts and elastomeric joints. This complex connection was a source of nonlinearity which contributed to test-model differences.
Solution
Proper identification of the nonlinear connection and creation of a nonlinear model allowed to properly represent the dynamics of the spacecraft structure.
Benefits
Efficiency gain.
Lower launch cost through safety margin and weight reduction.
We use cookies to ensure that we give you the best experience on our website. If you continue to use this site we will assume that you are happy with it.Ok
By continuing to use this website, you consent to the use of cookies in accordance with our Cookie Policy.